Had some work done today
Well.......................damn. LOL. That's my dawg. You get your stuff straight after your little catastrophy at the track? If my memory serves me correctly (usually doesn't), didn't you break a belt which made you overheat and warp a head? Been a while but not a long while and my short-term memory sucks. Hope she's alright.
Well.......................damn. LOL. That's my dawg. You get your stuff straight after your little catastrophy at the track? If my memory serves me correctly (usually doesn't), didn't you break a belt which made you overheat and warp a head? Been a while but not a long while and my short-term memory sucks. Hope she's alright.
I have the stock motor sitting in a crate in the garage. I haven't decided what I am going to do with it yet. I am either going to have the heads milled, cams installed and then heads installed or just sell it for whatever I can after having it all checked out.
The motor actually runs perfectly fine. I blew a head gasket most likely due to a warped head. It was pressurizing the coolant and blowing it out of the overflow on track. I caused me to spin on track when I blew coolant all over my wheel in turn 1. Most likely it needs the heads milled and head gaskets replaced.
I replaced the motor because I got a stupid deal on this one from a local shop. It was a fellow club members motor that had been machined and freshly rebuilt.
To be honest, I don't need the power so I will probably just sell it for suspension parts.
I replaced the motor because I got a stupid deal on this one from a local shop. It was a fellow club members motor that had been machined and freshly rebuilt.
To be honest, I don't need the power so I will probably just sell it for suspension parts.


